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DIY Steering stem nut Tool

12K views 23 replies 11 participants last post by  Nubby 
#1 ·
Ok...

Like many of you, I'm unwilling to pay the outrageous price that Suzuki wants for the Steering stem nut socket ($169 Cdn), so I decided to try and make my own.

I've seen some people use a grinder on a 1-1/4" deep socket, which was my original intention, however I couldn't find a deep socket for little $.

I then also saw Motophoria here on SVRIDER use some galvanized steel plumbing parts with some steel rod.

I managed to get my hands on a steering stem nut that I could use as a template...

So here's my take on the idea for less than $8US in parts...

I went into the plumbing section of my local hardware store, and grabbed:

- 1-1/4" threaded 4" galvanized steel pipe
- 1-1/4" to 1" galvanized steel reducer
- 1" galvanized steel threaded cap

Using a marker, I marked out the areas that had to be cut out using a locknut as a template. I also used a visual aid to show how much depth I needed to grind away.


I then grabbed some proper eyewear...


I placed the pipe in a vise, and using a grinder I ground away...


I used a file to clean up the edges and properly fit the nut




Once I knew I was as close as I'd get, I screwed the 3 pieces together using some steel epoxy. It's still drying, so I have yet to use it. I'm pretty sure it'll work just fine...



Oh yeah, the top cap can be used with an open end wrench, or a socket (I think 21mm or 22mm)

It's not as pretty as the Suzuki tool, but it will get the job done without mutilating the soft-as-butter aluminum locknut by using a hammer and a screwdriver.
 
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#10 ·
I usually grind a flat on to the side of the race with an angle grinder until it has a very thin spot. If you get it thin enough with out grinding into the stem you can then tap the race with a hammer and drift, it will fracture at the thinnest point, loosening up enough to slide it off.
 
#14 ·
Looks like a pretty good job, I'll have to check back to see how it works.

I'm also about to do a fork swap on my '03 SV and I also didn't want to buy a $70 socket.

I took my calipers down to Ace Hardware and measured a few sockets and found that a 1 1/4" twelve point deep socket with a 1/2" drive is just about the perfect size. It cost $8.79 US before tax. So there is another option for people who don't want to mess with epoxying pipe fittings.
 
#16 ·
I actually chose the 12 because it has less 'meat.'

A 1 1/4" 6 point socket is about 32 mm across, the flat parts of the castle nut are about 36 mm apart, so you would have to remove more material that way. The 12 point has more than enough material to work with.

When I'm done cutting the socket down I'll post some pictures, but this way you don't have to grind off as much material
 
#17 ·
Ok, so here's what I did:
First I took a dremel to the socket to remove the largest amount of material from between the teeth. I actually used 2 reinforced cutting disks with 2 high speed cutting disks sandwiched between them.

Then I used one of the nuts to mark the socket where the teeth needed to be




Next I used a flat file to remove the rest of the material. I feel like I can be more accurate with the file than with the dremel.


Here I am sizing up the teeth


And here is the finished product
 
#18 ·
EVERYONE,

The DIY tool I made to remove the steering stem castle-nuts was useless. It broke as soon as I applied some torque to it. The threaded pipe that I used is just too soft.

Those of you thinking of making your own tool, use a 1-1/4" deep socket as shown above by Neone, and not the pipe like i did.

I ended up using a large robertson screwdriver and a hammer, with suprisingly minimal damage to the nut.
 
#19 ·
Red-Line,

I wonder if your tool broke because the pipe threads weakened the "teeth" you cut. There's not much material left where the teeth are.

I'll bet you'd have better results if you cut off the threaded area and cut the teeth into the plain, unthreaded part of the pipe. I agree however, that starting off with an old deep socket would be a better bet.

... Gregg
 
#21 ·
When using the socket I modified I noticed that it was really easy for the socket to turn sideways while applying torque, but it worked just fine. The steel used in for the socket is very hard so if you cut it down by had be prepared to spend an hour or so filing it down.
 
#22 ·
If it's 36mm then why not just start with a 36mm socket instead of a 1.25"? I went and bought a 34mm tonight before coming home and seeing it was to short at the flat sides. It looks about 2mm short, ironic since I then found this post and will be exchanging it for a 36mm tomorrow...unless there's a good argument against starting with a 36mm, or I can't find one, but I believe O'Reilly's had one on the rack. I've got to get my bike finished, this is too depressing....

 
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